Mid Minnesota Truck Parts and Service

Mid Minnesota Truck Parts and Service Semi Tractor and Trailer Repair

For years I have looked at failure diagnosis charts and pictures and wondered if there is any possible way that these th...
06/13/2024

For years I have looked at failure diagnosis charts and pictures and wondered if there is any possible way that these things are actually possible. Well today, after 40 years, I have got one, so I have to share. I am left wondering... how much torque does it take to do this???

Hello!I just wanted to put a post out there that we have an E-Store, where you can look up parts, cross parts, and see p...
09/14/2023

Hello!

I just wanted to put a post out there that we have an E-Store, where you can look up parts, cross parts, and see pictures of what we have in stock! You can also put in an order online if you wish. If you have any questions, you can call Lindsey or Neal at (218) 430-0020. Hope every one is having a great week!

My daughter and I had some fun doing a little painting on this engine for my bus. Thanks for looking!
09/06/2022

My daughter and I had some fun doing a little painting on this engine for my bus. Thanks for looking!

Just ran across this one today. We are replacing the turbo for a new customer and found that the incorrect o ring was us...
11/13/2019

Just ran across this one today. We are replacing the turbo for a new customer and found that the incorrect o ring was used on this flat face connection. The o ring had too large of cross section. Lack of area in the flat face groove caused the o ring to be forced into the center of the fluid passage of the fitting when it was tightened. This is the turbo supply fitting. If any of the displaced material from the o ring had detached itself and entered the the turbo with the l**e oil, it would almost surely have sealed the fate of this turbo. Catastrophic failure of a turbo is never fun. Careful selection of o rings is critical. Someone got a lucky break on this one !

Recently rebuilt C15 for Eggert Farms. Had a lot of fun working on this engine and making it look extra awesome! Thanks ...
11/04/2019

Recently rebuilt C15 for Eggert Farms. Had a lot of fun working on this engine and making it look extra awesome! Thanks for looking :)

04/25/2015

I have not posted much lately, but this little problem took us a while to figure out. The problem is solved, Watch the short clip and post your ideas on what the issue was. Lets start a little conversation on what was going on here.

11/24/2014

Remember, simple stuff first. Had to share this shop issue. We had a customer purchase a new used truck, that he brought to us to repair before putting on the road. During that process, I suggested that he install a new set of injectors as there was a slight miss, hard start and fuming at idle. Engine ran well after injector install. Shortly after getting truck back, customer contacted us indicting that the engine was making oil. (crankcase oil level was rising not falling) We looked at engine, checking for cut o rings on injectors, fuel restriction, etc. and found nothing wrong. No change. We then replaced 2 injectors that were suspect. No Change. Customer was frustrated with our efforts to solve his issue, so took truck the the engine manufacturers distributor. They checked and said that they had found a rolled o ring on one injector. They then replaced all o rings on all injectors. No Change. They then replaced the injectors we had installed saying that they were bad. No Change. (We warranteed these injectors) They then suggested the cylinder heads be replaced as that is the last possibility. Customer asked that we take another look at this issue. We remove the fuel supply pump and found the shaft weep hole was wet, so had pump rebuilt. (this style pump is rarely and issue) No Change. We then ran engine on a dyed fuel mixture from an enclosed tank. This indicated that all of the (new) (new) injectors were leaking fuel from the top where the plunger enters the barrel. (This style injector has no seal at this location, and relies on a class fit (very tight tolerance fit) to control fuel flow at this point. This indicated a fuel return circuit restriction. We had checked this previously, but looked at it again. We again found no return circuit restrictions. We did identify a substandard fitting that we replaced. When replacing the fitting it was discovered that there was pressure in the tank as I took a fuel bath when disconnecting this fitting that was 1 foot above the fuel level. I checked with the customer and he indicated that he heard a hissing noise when removing the tank caps to fuel the truck. He said that he thought that it was suction noise not pressure. We tested a little further and found that two $30.00 tank breathers that were plugged, was the cause of thousands of dollars needless repair costs and was probably the reason that the truck was for sale in the first place. Patience and persistence will usually ultimately solve most problems. But the little things, overlooked, often cannot be solved with any amount of time or parts.

10/24/2014

Had another interesting situation in the shop this week. We had a customers truck in to replace a failed egr cooler. The cooler replacement went without a hitch. The fun began when cleaning the cooling system. When an egr cooler fails it allows the exhaust that it was designed to cool, to enter the cooling system, contaminating it with combustion byproducts. The procedure is to add cleaner and water to the cooling system and run vehicle down the road to raise the temperature and circulate cleaner through the entire system, drain, fill and repeat until system is clean enough to install antifreeze.
After the 2nd rinse, the truck refused to start. I connected the diagnostic computer and found an active fault for cam position sensor signal. Replaced sensor and sensor connector and truck started. After this rinse, truck again refused to start. Same cam sensor fault was active. Followed the trouble shooting tree through all the steps and found everything checked out. The last step in the tree said to ck if there had been any repairs to the timing gears or flywheel. Verify that these repairs had been performed correctly. This truck has had a couple clutches installed by another repair facility in the last month, so the flywheel had been off. I suspected that I would find a damaged crank position sensor ,from the flywheel hitting it during removal for clutch replacement.(this engine reads crankshaft position off from a notched tooth on the flywheel ring gear) After removing the sensor I found a piece of metal stuck to the end of the sensor because this sensor is magnetic. I removed the metal flake and re-installed the sensor. The truck started right up, and ran fine. No cam sensor fault. What happened??? After thinking about how the electronic control system works, it actually made sense. The larger surface area of the metal flake on the sensor tip made the signal sent to the computer a different pulse width than it was looking for. Because the crank sensor signal is the primary signal (reads a pulse every revolution) and the cam sensor is the secondary signal, (cam turns 1/2 speed of the crank) the computer assumed that the crank signal was correct.
But because the pulse width of the primary signal was different than it would have been without the larger (metal flake) surface area of the crank sensor, the computer assumed that the secondary signal from the cam sensor was incorrect causing the active fault code and thus the no start situation, when in reality there was nothing at all wrong with the cam sensor or sensor circuitry. The fun that we have without trying. You gotta love engine control electronics !!!!!!!!!!!!!!!!!!!

Did you ever wonder what happens when an oil cooler fails? This picture is the fluid that came out of the radiator of a ...
10/17/2014

Did you ever wonder what happens when an oil cooler fails? This picture is the fluid that came out of the radiator of a Cat C-13 acert truck engine with a failed oil cooler. An oil cooler has coolant running through cooler bundle tubes that are surrounded by engine oil, the coolant removes the heat from the engine oil. Some coolers have baffles that force the oil back and forth across the cooler bundle several times, increasing the efficiency of the cooler. Often the variation in oil pressure from normal engine operation, causes the baffles to move on the cooler tubes wearing them thin and eventually causing tube failure. Other coolers are designed with rubber sealing the tubes to the ends of the cooler housing. This rubber eventually cracks and fails. When either of these happen the oil usually ends up in the cooling system, because the oil pressure is higher than the pressure in the cooling system. This truck may have been the worst one we have ever done. After the cooler has been replaced, the cooling system needs to be cleaned. This one required using cooling system cleaner and test driving the vehicle, to bring the cooling system up to temperature, then draining and refilling and repeating the above process until the system is clean. This one required 7 flushes to clean.

10/09/2014

Just ran across something interesting in the shop today. Customer brought us a transmission that started grinding when shifting into low range. All control side functions ck'd out ok. After dis-assembly it was discovered that splitter gear and retainer were badly scored and the low side syncro friction material was badly worn. This type of damage is from towing the vehicle with out disconnecting the driveshaft. these transmissions are lubricated from the engine turning the internal gears and splashing the l**e inside the case, keeping all internal parts covered with l**e. When vehicles are towed it is typically when the engine is no longer running. When the output shaft turns but the rest of the transmission is not moving, the l**e is quickly spun off from the rotating parts, and severe wear and subsequent damage happens very quickly. These type failures are preventable by taking the time to make sure the transmission output shaft is not turning during the towing process. This applies to almost all transmissions. Manual or automatic. Driveshafts or axle shafts need to be removed when towing with the tires on the ground.

10/07/2014

For those of you that haven't serviced your air dryer yet, the effective time to do so is all but gone. If the air system is wet it needs to have dry air run through if for a period of time in order to move the moisture out and dry it back out. Servicing the dryer after the weather is below freezing will do nothing to help a wet system,but prevent any additional moisture from entering, it will not help remove the moisture trapped in the system. The best time of the year to service an air dryer is in July or August. The best way to see if your system is wet is to manually drain the air from the (wet) first tank after the air dryer. If it show any signs of moisture, your air dryer needs service. Or if it has not been serviced in the last 2 years. One other note. if you need to add air brake anti freeze to the system, make sure that you do NOT run it through the air dyer. Alcohol can break down the desiccant inside the dryer.

Address

1034 Ash Avenue NE
Wadena, MN
56482

Opening Hours

Monday 8am - 6pm
Tuesday 8am - 6pm
Wednesday 8am - 6pm
Thursday 8am - 6pm
Friday 8am - 6pm

Telephone

+12184300020

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